摘要
介绍定量化注采调整方法及其在七棵树油田的应用。七棵树油田于2015年下半年进行了定量化调整试验。利用定量化计算结果,结合油藏数值模拟,对SW10区块主要控制油井井间干扰,调整驱替压力;对SW8区块主要优化油水井井间流线,实现油藏均衡水驱。试验取得了较好的效果,油田产油量由62 t/d上升到了74 t/d。
The quantitative injection-production adjustment method and its application are introduced in this paper in Qikeshu Oilfield. In the second half of 2015, quantitative adjustment experiments are carried out in Qikeshu Oilfield. According to quantitative calculation results and reservoir numerical simulation, the interwell interference is mainly controlled in SW10 block, and displacement pressure is adjusted. And the interwell streamline of SW8 block is optimized to realize balanced water flooding. Good results have been achieved and the daily oil production of the oilfield has increased from 62 t/d to 74 t/d.
引文
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