氮封微压气浮在焦化含硫污水中的应用
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  • 英文篇名:Application of N_2-sealed Micro Pressure Flotation in Treating Sour Water From Delayed Coker
  • 作者:周建文
  • 英文作者:Zhou Jianwen;Sinopec Jinling Company;
  • 关键词:延迟焦化 ; 氮封微压气浮 ; 含硫污水 ; 脱焦粉 ; 脱油
  • 英文关键词:delayed coking unit;;nitrogen sealed micro pressure floatation;;sulfur-containing wastewater;;removing coke powder;;removing oil
  • 中文刊名:WZSH
  • 英文刊名:Green Petroleum & Petrochemicals
  • 机构:中国石油化工股份有限公司金陵分公司;
  • 出版日期:2017-04-20
  • 出版单位:石油石化绿色低碳
  • 年:2017
  • 期:v.2;No.8
  • 语种:中文;
  • 页:WZSH201702011
  • 页数:3
  • CN:02
  • ISSN:10-1378/TE
  • 分类号:46-48
摘要
针对炼油厂延迟焦化装置含硫污水含有焦粉细微颗粒、油类以及硫化物的特点,研发出一体化氮封微压气浮工艺,在处理焦化装置50 m~3/h含硫污水时,油脱除率为50.39%,COD脱除率为13.62%,固体悬浮物(SS)浓度脱除率为82.61%,浊度下降了92.87%,油含量小于300 mg/L,SS浓度不大于50 mg/L,运行费用约1.33元/m~3废水,减少了含硫污水罐回收油量,延长了污水汽提装置的生产周期。
        In order to deal with the sour water containing fine particles, oil and sulfide from delayed coking unit, an integrated nitrogen-sealed micro-pressure air floatation process has been developed. In treatment of the sulfurcontaining wastewater 50 m~3/h from the coking unit, the process can achieve following results: oil removal rate at 50.39%, COD removal rate at 13.62%, SS removal rate at 82.61%, turbidity reduction by 92.87%, oil content less than 300 mg/L, SS concentration less than 50 mg/L, operating cost about 1.33 yuan/m~3 wastewater, reduced oil for recovery in the sulfur-containing wastewater tank, and extended operation cycle of the wastewater stripping unit.
引文
[1]彭刚,何永强,汪泽龙.VF–1200立式密闭氮气气浮在高Ⅱ联污水处理中的应用[J].内江科技,2009(2):129.
    [2]郭学峰,王和琴,赵广胜.高含硫油气田含硫废液的达标处理回注方法[J].工业水处理,2013(5):86.

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