多层泄孔运行方式对二级斜坡进口浅水垫消力池水力特性的影响
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  • 英文篇名:Influence of Operation Model of Multi-layer Discharging Holes on Hydraulic Characteristics of Stilling Basin with Two-stage-slope Inlet Shallow-water Cushion
  • 作者:魏晶晶 ; 李连侠 ; 张法星 ; 廖华胜 ; 李秋林 ; 唐玉川 ; 易文敏 ; 沈焕荣
  • 英文作者:WEI Jing-jing;LI Lian-xia;ZHANG Fa-xing;LIAO Hua-sheng;LI Qiu-lin;TANG Yu-chuan;YI Wen-min;SHEN Huan-rong;State Key Laboratory of Hydraulics and Mountain River Engineering,Sichuan University;Michigan State University;
  • 关键词:泄洪消能 ; 消力池 ; 运行方式 ; 二级斜坡进口
  • 英文关键词:energy dissipation;;stilling basin;;operation mode;;two-stage-slope inlet
  • 中文刊名:SDNY
  • 英文刊名:Water Resources and Power
  • 机构:四川大学水力学与山区河流开发保护国家重点实验室;密歇根州立大学;
  • 出版日期:2019-04-25
  • 出版单位:水电能源科学
  • 年:2019
  • 期:v.37;No.224
  • 基金:国家自然科学基金项目(51079091,51209154);; 国家重点研发计划(2016YFC0401705);; 四川省青年科技创新团队专项计划(2016TD0020)
  • 语种:中文;
  • 页:SDNY201904028
  • 页数:4
  • CN:04
  • ISSN:42-1231/TK
  • 分类号:115-118
摘要
针对某水电站工程消力池体型不合理及调度运行方式不当而导致池内流态不良、消力池临底流速过大、底板冲刷破坏等问题,通过1∶45模型试验分析了二级斜坡进口式浅水垫消力池在多层泄洪孔不同运行方式下的水力特性。结果表明,新提出的消力池体型能够明显改善面流流态及水跃不稳定等问题,针对该工程,优先采用溢流表孔泄流比采用冲沙底孔泄流池内流态更佳,消力池临底及岸边流速更低,消能防冲效果更好。
        To solve the problems of bad flow regime and large bottom velocity caused by unreasonable design of stilling basin and improper operation mode of a certain hydropower project with multi-layer discharging holes,a new type of SBWWC with two-stage-slope inlet was proposed and a hydraulic model test with scale 1∶45 was conducted to compare the effects of different operation mode of the discharging holes on the hydraulic characteristics of the stilling basin.The results show that the newly proposed stilling basin can significantly improve the situation of the surface flow regime and instability of hydraulic jump.For this project,it is better to use overflow surface holes than the bottom holes to release flood from the view of energy dissipation.The flow regime is better,the bottom velocity and the shore velocity is lower.
引文
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