上汽-西门子超超临界1000MW汽轮机的优化运行
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  • 英文篇名:Optimized Operation of SAIC-Siemens Ultra-supercritical 1 000 MW Steam Turbines
  • 作者:孙永平 ; 童小忠 ; 包劲松 ; 秦攀
  • 英文作者:SUN Yongping;TONG Xiaozhong;BAO Jinsong;QIN Pan;Electric Power Research Institute,State Grid Zhejiang Electric Power Company;
  • 关键词:1 ; 000MW汽轮机 ; 通流特性 ; 节能分析 ; 优化运行 ; 试验研究
  • 英文关键词:1 000MW steam turbine;;flow characteristic;;energy-saving analysis;;operation optimization;;experimental study
  • 中文刊名:DONG
  • 英文刊名:Journal of Chinese Society of Power Engineering
  • 机构:国网浙江省电力公司电力科学研究院;
  • 出版日期:2014-03-15
  • 出版单位:动力工程学报
  • 年:2014
  • 期:v.34;No.231
  • 语种:中文;
  • 页:DONG201403005
  • 页数:5
  • CN:03
  • ISSN:31-2041/TK
  • 分类号:33-36+46
摘要
为了提高上汽-西门子超超临界1 000MW汽轮机的运行性能,进行了汽轮机高、中、低压缸通流效率变化特性试验,并以试验结果分析为基础,针对性地开展了机组运行优化研究.通过汽轮机进汽端不同滑压方式的试验比较,确定了机组滑压优化控制曲线,降低了汽轮机高压调门的节流损失;通过开发基于SIS平台的冷端优化管理系统,指导运行人员按照收益与成本比较排序结果来确定循环水泵等冷端设备的优化运行方式,实现了冷端运行效益的最大化;针对汽轮机第六级抽汽的2根管道存在温度偏差的问题,在管道外壁加装了隔热套,将管内蒸汽温度提高10K以上,消除了管内积水隐患.在试点1 000MW汽轮机上的实际应用结果表明:这些优化改进措施的实施不同程度地提高了机组运行的安全性与经济性.
        To improve the operation performance of SAIC-Siemens ultra-supercritical 1 000MW steam turbines,performance tests were carried out to the HP/IP/LP turbine casing so as to obtain their flow efficiency,based on which operation optimization was studied for the unit.The throttling loss of high-pressure control valve was reduced by comparing the sliding pressure operation modes and optimizing the sliding pressure operation curves at turbine inlet end.The cold-end effect was maximized by developing an SIS platform-based cold-end optimization management system to guide operators to determine optimal operation mode of cold-end equipment,like circulating water pump,according to comparing and sorting results of related benefit-cost model.To solve the temperature deviation problem existing in two pipes at stage 6,insulation covers was added to external wall of the pipes to increase the inside steam temperature by 10K,eliminating the hidden trouble of internal water accumulation.Application results to a 1 000MW steam turbine indicate that the implementation of above optimization and improvement measures has to some extent helped to improve the operation safety and economical efficiency of the unit.
引文
[1]包劲松,孙永平.1 000MW汽轮机变负荷运行经济性比较分析[J].浙江电力,2011,30(4):1-3.BAO Jinsong,SUN Yongping.Economical comparison and analysis on variable load operation of 1 000MW units[J].Zhejiang Electric Power,2011,30(4):1-3.
    [2]范鑫,秦建明,李明,等.超临界600MW汽轮机运行方式的优化研究[J].动力工程学报,2012,32(5):356-361.FAN Xin,QIN Jianming,LI Ming,et al.Study on operation mode optimization for a 600 MW supercritical steam turbine[J].Journal of Chinese Society of Power Engineering,2012,32(5):356-361.
    [3]孙永平,童小忠,樊印龙.600 MW机组滑压运行方式优化的试验研究[J].热力发电,2007,36(8):66-68.SUN Yongping,TONG Xiaozhong,FAN Yinlong.Test study on optimization of sliding pressure operation mode for 600MW units[J].Thermal Power Generation,2007,36(8):66-68.
    [4]李蔚,马洁,盛德仁,等.大型火电机组冷端优化在线指导系统的研究[J].浙江电力,2011,30(9):34-37.LI Wei,MA Jie,SHENG Deren,et al.Research on online guidance system for optimization of cold-end system in large scale thermal power unit[J].Zhejiang Electric Power,2011,30(9):34-37.

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