某电厂燃气轮机功率振荡事件分析和处理
详细信息    查看全文 | 推荐本文 |
  • 英文篇名:Analysis and Treatment of Power Oscillation Incident in a Gas Turbine Plant
  • 作者:刘锡海
  • 英文作者:LIU Xihai;Shenzhen Energy Group Limited Eastern Power Plant;
  • 关键词:燃气轮机 ; 功率振荡 ; PSS
  • 英文关键词:gas turbine;;power oscillation;;PSS
  • 中文刊名:GXDL
  • 英文刊名:Guangxi Electric Power
  • 机构:深圳能源集团东部电厂;
  • 出版日期:2017-12-28
  • 出版单位:广西电力
  • 年:2017
  • 期:v.40;No.168
  • 语种:中文;
  • 页:GXDL201706016
  • 页数:5
  • CN:06
  • ISSN:45-1307/TK
  • 分类号:61-65
摘要
对某电厂燃气轮机功率振荡事件进行分析。通过现场检查,发现燃气轮机输出的有功功率振荡是由燃气流量控制阀、燃气压力调节阀磨损、松动引起的。单机有功功率振荡还导致了无功功率的大幅振荡,其原因是励磁系统的PSS采用了PSS1A模型。为了避免类似事件再次发生,建议加强燃气流量控制阀、燃气压力调节阀的解体检修,此外,作为调峰或日起停的燃气轮机组,其PSS不适宜采用PSS1A模型。
        A power oscillation incident in a gas turbine plant is analyzed. By field inspection, it is found that the output of active power oscillation from the gas turbine is caused by the abrasion and loose of the gas flow control valve and the gas pressure control valve.The active power oscillation of single unit also caused the large scale of reactive power oscillation, which is because of the usage of PSS1A model in the PSS of excitation system. In order to avoid similar incident happening again, it is suggested that the overhaul of the gas flow control valve and the gas pressure control valve be strengthened, and the PSS1A model is not suitable to be used in the PSS of gas turbine unit if it is used as the peak regulation or the daily starting & stopping unit.
引文
[1]孟凡超,吴龙.发电机励磁技术问答及事故分析[M].北京:中国电力出版社,2008.
    [2]张仰飞,袁越,陈小虎,等.有功型PSS抑制低频振荡机理及反调特性[J].电力系统保护与控制,2010,38(3):77-80.

© 2004-2018 中国地质图书馆版权所有 京ICP备05064691号 京公网安备11010802017129号

地址:北京市海淀区学院路29号 邮编:100083

电话:办公室:(+86 10)66554848;文献借阅、咨询服务、科技查新:66554700