催化裂解装置烟气除尘水处理系统运行分析
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  • 英文篇名:Operation analysis of water treatment system of flue gas dust removal in catalytic cracking unit
  • 作者:冯兴 ; 郝明生 ; 王保华
  • 英文作者:Feng Xing;Hao Mingsheng;Wang Baohua;CNOOC Ningbo Daxie Petrochemical Co.;
  • 关键词:催化裂解 ; 烟气 ; 除尘 ; 水处理
  • 英文关键词:catalytic cracking;;flus gas;;dust removal;;water treatment
  • 中文刊名:LYSZ
  • 英文刊名:Petroleum Refinery Engineering
  • 机构:中海石油宁波大榭石化有限公司;
  • 出版日期:2019-05-17 15:33
  • 出版单位:炼油技术与工程
  • 年:2019
  • 期:v.49;No.403
  • 语种:中文;
  • 页:LYSZ201905003
  • 页数:4
  • CN:05
  • ISSN:41-1139/TE
  • 分类号:14-17
摘要
催化裂解再生烟气中含有大量的SO_x,NO_x和颗粒物,会对所在区域环境造成较为严重的污染。随着目前环保形势日益严峻,国家对废气、废水排放指标提出更加严格的要求,设置脱硝除尘系统成为必然。大榭石化2.2 Mt/a催化裂解装置烟气除尘水处理系统于2016年6月与主体装置同步开工以来,一直运行良好。烟气除尘系统采用湿法除尘脱硫技术,烟气经净化处理后,烟气粉尘质量浓度可降至20 mg/m~3,SO_x质量浓度降至10 mg/m~3。外排污水经水处理系统沉淀氧化后,悬浮物质量浓度为22 mg/L,化学需氧量COD为20 mg/L,pH值控制在6~9,均能满足环保要求。系统运行过程中,出现了洗涤塔除沫网被腐蚀、外排含盐污水COD异常偏高、氧化罐结垢和出口含盐污水pH值偏高等问题,通过对存在问题进行分析和总结,采取了有效解决措施,保证了装置平稳运行。
        The regenerated flue gas from catalytic unit cracking contains a large amount of SO_x, NO_x and particulate matter, which will cause serious pollution to the environment in the region. With the increasingly serious environmental protection situation, the state has put forward stricter requirements for the emission index of waste gas and wastewater, and it is necessary to set up a denitrification and dust removal system. The water treatment system of flue gas dust removal of 2.2 MM TPY catalytic cracking unit in CNOOC Ningbo Daxie Petrochemical Co. has been running well since it was started synchronously with the main device in June 2016. The wet dedusting and desulphurization technology is adopted by flue gas dust removal system. After purification, the mass concentration of flue gas dust can be reduced to 20 mg/m~3 and the mass concentration of SO_x can be reduced to 10 mg/m~3. After sedimentation and oxidation in water treatment system, the concentration of suspended substance is 22 mg/L, COD is 20 mg/L and pH value is 6~9, which can meet the environmental protection requirements.During the operation of the system, problems such as corrosion of the foam removal network of the scrubbing tower, exceptionally high COD in effluent of saline sewage, scaling of the oxidation tank and high pH value of the saline sewage from the outlet arise. Based on the analysis and summary of the existing problems, effective measures are taken to ensure smooth running of the unit.
引文
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