摘要
对2片不同轴压比的装配式空心剪力墙进行了拟静力试验,描述了该墙的破坏过程,分析了墙体的破坏特征、滞回特性、耗能能力等抗震性能。结果表明,装配式空心剪力墙主要呈弯剪破坏;随着轴压比的增大,墙体承载力增大,延性提高,耗能能力提高,刚度退化加快;装配式空心剪力墙的抗震性能良好,应用于三层及以下低轴压比结构时,具有较大的安全储备。最后,结合试验结果与相关文献结论,给出了该结构形式的装配式空心剪力墙的弹性刚度计算式修正系数。
The quasi-static experiment was conducted on 2 pieces of prefabricated hollow shear walls with different axial compression ratios. The failure process of the wall was described,and the seismic performance such as the failure characteristics,hysteresis characteristics and energy dissipation capacity of the walls were analyzed. The results show that the prefabricated hollow shear wall suffers from bending and shear failures. With the increase of the axial compression ratio,the bearing capacity of the wall is increased,the ductility is improved,the energy dissipation capacity is improved and the rigidity degradation is accelerated. The seismic performance of the prefabricated hollow shear wall is good,and it has large security reserves when it is applied to the structure with three layers or less under low axial pressure ratio. Finally,the correction coefficient of elastic stiffness calculation formula of the prefabricated hollow shear wall was given in combination with the experimental results and the related literatures.
引文
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