重钢铁水喷粉脱硫工艺优化研究
详细信息    本馆镜像全文|  推荐本文 |  |   获取CNKI官网全文
摘要
本论文对重钢铁水进行了不同脱硫剂脱硫的对比实验室研究;在此基础上筛选出适合重钢条件的三种类型即CaO系、CaO-AD系复合脱硫剂和CaO-Mg系复合脱硫剂,对其进行了工业性试验,为大生产提供经济、实用的脱硫剂配方;同时对喷吹脱硫工艺参数进行了优化,建立脱硫粉剂消耗预测模型,并对脱硫后在铁包和转炉冶炼中的回硫问题及低硫钢的冶炼进行了研究;最后,对CaO+Mg石灰基混合喷吹进行了脱硫能力及综合消耗工业性扩大试验研究。主要结果为:
     (1)通过对CaO系、CaO-AD系和CaO-Mg系三种脱硫剂实验室实验和热力学分析,得出脱硫能力从大到小排序是:CaO-Mg系→CaO-AD系→CaO系。
     (2)通过工业性试验后确立了适应重钢条件的脱硫剂类型是:中度脱硫剂为CaO石灰基;深度脱硫剂为CaO+Mg基。
     (3)针对重钢炼钢厂脱硫现状存在的问题,在配方确定的基础上对脱硫工艺参数进行优化,取得了比较满意的冶金效果,处理成本下降了5.991元/吨铁,经济和社会效益明显。
     (4)脱硫粉剂消耗数学模型的建立,采用石灰基脱硫,目标硫确定在0.006~0.010%内,消耗相对误差不超过5%,克服无模型前加料盲目的弊端,对提高脱硫命中率和降低生产成本发挥出重要作用。
     (5)脱硫铁水在铁包内回硫的控制因素主要有三方面:喷枪结构、后搅工艺和铁水等待时间;通过正交实验法,得出影响重钢脱硫铁水在转炉内回硫的首要因素是废钢质量,再者是扒渣好坏,最后是石灰质量。保证最小回硫量的低硫钢生产方案是:扒渣好——低硫废钢——气烧低硫石灰。
     (6)低硫钢冶炼实验证明:采用“石灰基铁水脱硫——转炉冶炼——吹氩——连铸”工艺路线,重钢炼钢厂已具备生产成品硫≤0.015%低硫钢的能力。
     (7)CaO+Mg混合喷吹实验,处理结束[S]<0.005%;相对石灰基础脱硫,粉剂消耗下降2kg/t,处理时间缩短3min,温降减少17℃以上。存在的不足是脱硫剂中Mg偏析严重,渣铁分离相对困难。
In this paper,the compared experiment of desulphurization of hot metal of Chongqing Iron and Steel Co.(in short CQ),which is used by different desulphurizing agents,has been carried out in lab. On the base of the experiment,it is selected three type desulphurizing agents that fit the production condition of CQ have been carried out for industrial experiment,which are CaO-based,CaO-AD-based and CaO-Mg-based synthetic desulphurizing agent. It provided an economical and practical scheme of desulphurizing agent for product line. Meanwhile,the injection technologic parameters have been optimized,and a forecast model of consuming desulphurizing agent has been developed. The smelting resulfurization and smelting low-surphur steel in jar and converter after hot metal desulphurization have been researched. Finally,desulphurization capacity and entire consuming of Mg and CaO-based desulphurizing agent mixed insufflating have been on ampliative and industrial research. Then the conclusions can be drawn as following:
    (1)Through the experiments in lab and the thermodynamics analysis of the three types desulphurizing agents,which are CaO-based,CaO-AD-based and CaO-Mg-based desulphurizing agent,it can be gained that the array order of the desulphurization capacity from the stronger to the weaker is:CaO-Mg-based-CaO-AD-based - CaO-based.
    (2)The type of desulphurizing agent fit the production condition of CQ has been confirmed though the industrial experiment. Medium desulphurizing agent is CaO-based and deep desulphurizing agent is Mg plus CaO-based.
    (3)Aiming at the actual problem in desulfurization process of CQ,the desulphurization technologic parameters have been optimized on the basis of confirming the scheme. It is obtained approving metallurgical effect. Disposal cost has declined 5.991 yuan per ton steel,and the economic and social benefit is obvious.
    (4) With the foundation of consuming desulphurizing agent model,by using CaO -based desulphurizing agent,target sulfur is in the range of 0.006-0.010,and consuming fractional error has not been exceeded 5%. The unreasoning disadvantage of charging before having the model has been overcame. It is important for increasing the desulphurization rate and declining the production cost.
    (5) The control factors resulfurized of the desulphurizing hot metal in ladle have three important aspects:the structure of lance,the process after disturbing and the waiting time of hot metal. Through orthogonal experiment method,it can be obtained that the scrap quality is the chiefly factor to affect resulfurized of the desulphurizing hot metal in the converter at the steelworks in CQ:The second factor is decided by the slag removal which is better or not;The last factor is decided by lime quality. The best production scheme of low-sulfur steel,which can ensure lowest the resulfurization quantity,is:the high quality of slag removal,low-sulfur scrap,low-sulfur lime burnt by gas.
    (6)The low-sulfur steel experiments can prove that the steelworks in CQ has the capacity of producing the low-sulfur steel for the sulfur content less than 0.015% of the finished products by using the technical process of "desulfurization hot metal with CaO-based,converter smelting,argon-bubbling treatment and continuous casting. "
    (7)The experiment of insufflating Mg and CaO-based desulphurizing agent had been carried out. It can be obtained that the final point [S] could achieve 0.006-0.010%. Comparing the CaO-based desulphurizing agent,the consumed amount of powder reagent could be decreased 2 Kg per ton,the disposal time could be saved 3 minutes,and the reduced temperature could be decreased more than 17 C. The shortage of the experiment is Mg in the desulphurizing agent has great segregation,and it is
    
    
    correspondingly difficult for separating slag from hot metal.
引文
1.杨天钧,高征铠等,铁水炉外脱硫的新进展,钢铁,1999(01):P65~69
    2.ESM Inc编著,铁水预处理用高效复合脱硫粉剂,攀钢技术,1995,5(18):P14~19
    3.狄文范,铁水炉外脱硫技术的发展概况,钢铁,1991(10):P68
    4.欧阳守忠,铁水脱硫预处理方法及其有关新技术的发展,炼钢,1995(03),P61
    5.北美铁水预处理脱硫进展,世界金属导报,1998(12):8
    6.铁水预处理新工艺,世界金属导报,1998,11.03
    7.徐大全,铁水炉外预处理,北京,冶金工业出版社,1988(07):P1~3
    8.张荣生,钢铁生产中的脱硫,北京,冶金工业出版社,1986(04)
    9.野见山赛,市川浩,丸川雄净,铁钢,1983,P69:1738
    10.罗小刚,钒钛铁水的预处理研究,1999(05)
    11.平原宏章,山崎,铁钢,1979,P65:221
    12.梁连科,杜钢,铁水预处理工作的发展,辽宁冶金,1997,(2)
    13.徐愚,日本铁水预处理进展情况简介,宝钢情报,1989增刊·P21~25
    14.李宏鸣等,铁水脱硅、脱硫、脱磷试生产实践与分析,钢铁,1992,9:5~10
    15.林企普,铁水脱硅、脱硫、脱磷处理技术开发应用,钢铁,1992,(9):P11~15
    16.魏庆成,冶金热力学,重庆大学出版社,1996:P142~263
    17. Bieniosek Thomas.Hot Metal Desulfuriza Desulfurization by co—injection of calcium Carfide and Magnesium. Steelmaking Conference proveedings, 1986, 69:P349~356
    18.张信昭,喷粉冶金基本原理,北京,冶金工业出版社·1988:P1~294
    19.中村博已,三田见三方.铁钢,1982,68:946
    20. K. Sassaki et al. Submitted to the 66th Steeelmaking Conference of AIME in Atlanta. 1983
    21. Zhao Y F and Irons G A.Sinmultaneous Desulfurization and Deonidation. Ironmaking and Steelmaking, 1994, 2k47: P10~15
    22.黄希祜,钢铁冶金原理,北京,冶金工业出版社,1989
    23.黄焕程,攀钢铁水脱硫工艺的进步与发展,炼钢,1989(06):6~9
    24.万德光,张善楚,金属镁在铁水炉外脱硫中的应用,炼钢,1989(01):P7~14
    25. K. Lovald, Ironmaking and Steelmaking, 1980, No. 1
    26.李吹宣,镁钙系列铁水脱硫技术及经济分析,炼钢,1997,Vol32.No.11
    27.陈家祥编著,炼钢常用图表数据手册,北京,冶金工业出版社,1984(11),40
    28. Engh T A etal.Thermedynamic of the reaction between magnesium and sulfur in carbon saturted iron at 1260℃.scandina journal of metallargy, 1979(8):P195~198
    29. Vaminaski j h.lime and magnesium co-injection for efficient desulfurization of hot metal, 1982(4):P165~173
    30.万否志郎等,融体精炼反应与基础应用,西山记念技术讲座,昭和63:P3~293
    31.攀钢钢铁研究院,含AD粉石灰基脱硫剂的研究,1998(11)
    
    
    32.夏辛明,混铁车内铁水脱硅、脱磷、脱硫的生产实践,钢铁,1999(10):P547~560
    33.吴引淳,铁水脱硫的热力学与动力学浅析,炼钢,1996(02)
    34.J.c.aurual,用镁进行铁水脱硫的经济效益,Iron and steelmaker,1984(05):P40~44
    35.谢效方,单玲玲等,CaO基粉剂的铁水脱硫试验,钢铁,1989(09)P12
    36. Toshiyasu ohnishi et al. pretreatment technique of hot metal by newly developed refining furnace, 神户制钢技报·38 (1): P9
    37.车传仁,第一届全国炉外预处理会议论文集,中国金属协会,1992(10):P21~27
    38. Katsuma yoshida et al. development of effective retining process consisting of both hot metal pretreatment and decarbarization in two top and bottom converters, 铁钢, 1990(11): P1817
    39. Kouichi torii et al. Improvement of dephosphorization capacity in srp.camp-isv, 1998(11):P142
    40.陈家祥,钢铁冶金学(炼钢部分),北京冶金出版社,1990:P9~15
    41.刘守平等,铁水用金属镁脱硫的热力学分析,钢铁钒钛,1998(03):P16~19
    42.张荣生,钢铁生产中的脱硫,北京,冶金工业出版社,1986:P98~104
    43. Derusha g.e et al. sequenced iron desulfurization by calium carbide/magnesium co-injection, steelmaking conference proceedings, 1990, 73:P351~355
    44. Bieniosek Thomas. hot metal desulfurization by co-injection of carbide and magnesium, steelmaking conference proceedings, 1986,69:P349~356
    45. Rolinson s wan, Improved sequenced co-injectiong practice for blast furnace hot metal desulfurization, steelmaking conference proceeding. 1995,78:P183~189
    46. Shuei etal, Development of steelmaking Process with nunumum slay generatim in No.3sms. Fukuyama warths. CAMP-ISIJ.1998(11) :P144
    47. Sohn ho-sang etal, hot metal pretreatment in a converter, camp-isij. 1997(10) :P781

© 2004-2018 中国地质图书馆版权所有 京ICP备05064691号 京公网安备11010802017129号

地址:北京市海淀区学院路29号 邮编:100083

电话:办公室:(+86 10)66554848;文献借阅、咨询服务、科技查新:66554700