摘要
针对某钢厂200 mm×200 mm的65Mn铸坯存在脱方、角部凹陷和三角区裂纹等质量问题,通过分析缺陷是由结晶器及二次冷却不均造成的,提出扩大结晶器铜管R角、锥度及增加二冷水量工艺优化方案,扩大结晶器铜管R角及锥度改善结晶器冷却传热,增加二冷水量提高足辊水压,使得二冷段喷淋冷却效果更好,提高铸坯冷却均匀性,铸坯脱方、角部凹陷和三角区裂纹等缺陷明显改善,铸坯质量得到大幅提高。
There is off-square,angle concaves and corner cracks in 200 mm square billet of 65 Mn in a certain steel plant,which are caused by the uneven cooling of mold and secondary cooling zone by analyzing. The process optimization schemes of enlarging the R Angle and the taper and increasing the secondary cooling water flow have been carried out. The method of enlarging the R Angle and the taper of the mold improve the heat transfer of the mold cooling. The increase of the secondary cooling water and the water pressure of the foot roller improve the cooling effect of the secondary cooling section. The cooling uniformity of casting billet has been increased. The test shows the quality problems of off-square,angle concaves and corner cracks have been controlled effectively and the quality of casting billet has been greatly improved.
引文
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