摘要
针对某台600MW汽轮发电机组定速3000r/min后出现的不稳定振动进行分析诊断,确定造成不稳定振动的原因是低压轴端汽封动静碰摩,轴瓦支撑刚度低,密封瓦碰摩,滑环轴存在不平衡质量及碳刷碰摩等,采取了提高发电机密封油油温,滑环轴热态动平衡等处理措施,消除了不稳定振动。
To diagnose the unsteady vibration occurred on a 600 MW unit, after fixed speed3000 r/min. It's found out that the cause of the unsteady vibration of the turbine is impact-rubbing between the gland seal of LP shaft and rotating shaft, low support dynamic stiffness of bearing,impact-rubbing of sealing pad, unbalance of slip ring shaft, and impact-rubbing of carbon brush etc.By increasing the tempreture of sealing oil of generator, thermal dynamic balance of slip ring shaft etc. the unsteady vibration of the turbine is eliminated.
引文
[1]刘石.轴承座热态标高变化的振动特征识别与诊断[J].汽轮机技术,2004,46(5):379-381.
[2]施维新.汽轮机工作转速下转轴碰摩振动及其诊断[J].中国电力,1994(6):28-34.
[3]何国安,王忠安,张卫军,等.1000MW汽轮机低压缸动静碰摩分析与处理[J].热力透平,2013,42(1):58-61.
[4]冯永新,刘石,邓小文.某660MW机组中低压转子振动故障原因分析与处理[J].汽轮机技术,2009,51(3):226-228.
[5]施维新,石静波.汽轮发电机组振动及事故[M].中国电力出版社,2008.
[6]施维新.柔性转子轴系平衡技术的发展[J].中国电力,2011,44(2):31-36.
[7]何国安,闵昌发,张学延,等.国产600MW汽轮发电机组轴系动平衡研究[J].动力工程学报2012,32(4):282-288.
[8]高庆水,刘石,张楚.汽轮机座缸式轴承振动影响因素研究[J].振动与冲击,2014,33(13):26-30.
[9]张学延.汽轮发电机组振动诊断[M].中国电力出版社.
[10]施维新.浮动和接触密封对轴系振动影响的测试及分析[J].中国电力,2004,37(2):11-16.
[11]李录平,晋风华,游力元,等.汽轮发电机组起动过程振动故障诊断与处理措施[J].热力发电,2006(11):37-41.
[12]刘石,刘兴久,冯永新,等.超临界600MW机组检修后振动分析及处理[J].振动、测试与诊断,2009,29(4):406-409.
[13]刘石,王飞,冯永新,等.引进型600MW发电机组轴系振动特征及处理[J].大电机技术,2009(5):4-12.
[14]寇胜利,尹赐君.元宝山电厂600MW发电机的振动[J].大电机技术,2003(6):20-25.
[15]寇胜利.发电机的现场动平衡[J].大电机技术,2006(1):14-22.
[16]王延博,李甲伟,杨青.600MW机组轴系振动故障诊断及处理[J].热力发电,2012,41(8):59-61.